Jump to content

Rob

BMT Benefactor
  • Posts

    12,753
  • Joined

  • Last visited

  • Days Won

    175

Everything posted by Rob

  1. I am thinking of towing a guy's truck to a show and it is a couple hundred miles away. I would need to do this with a tow bar. The truck has a quadraplex transmission. I know these have an oil pump inside but I'm wondering if it is driven by the input shaft, when the engine runs, or by the ouput shaft when the transmission is turning internally? I could let the engine idle the whole way but that is several hours which I know would not hurt as long as the towing unit did not impede sufficient air through the radiator core. Thanks, Rob
  2. Bill, go to OldMacksRus.com. The transmission data is there. Rob
  3. I was originally looking at that item also but when I look at my "engine stock", I really don't need it. I never received a return message from the seller on anything I had asked including how long it had been removed from the truck. The ad did not say anything about the condition, nor experience with the truck. The weight is about 2500 lbs hooked together with all the ancillary equipment as shown. The Mack engines are fairly lightweight compared to others. What would you do with something like this when completed? It could be an interesting project but remarketing with a loss in time and money is a strong possibility. Good luck to you in the perseverance of a project. Rob
  4. Hi Larry, thanks for the input. I do not know if there are spacers or not. The pan gasket appears to be fairly new, (under all the grease buildup) and I've not had it apart. It only leaks at the one bolt and I've done nothing with it yet. Thanks, Rob
  5. Man, I've got to quit reading this board so late at night....... I find it hard to sleep when I'm grinding on an idea. I arrived to the shop early this morning about 5:30 am and took after the throttle linkage. It adjusted right down to stalling the engine if I wanted to. Ultimately, it idles at 644-648 rpm via my hand held electronic tachometer, (it is accurate). If the engine is revved to approximately 1000 rpm, and the throttle released, the engine decelerates to 639-641 rpm and immediately stabilizes at the above mentioned figures. I did not realize that a mechanical governed engine would be that "tight" in speed regulation. I maintain standby powerplants so speed regulation is familiar to me. Now when my tool bit for the leaking buttess screw shows up......... Rob
  6. Hi Michael and FJH, I wanted to say "thank you" to you both personally as your input was the inspiration to make this thing right. All of the input received was positive inspiration as I have a hard time living with something that is not "quite right". If I have an inkling of bettering something, I usually jump right in. It really was fairly easy to machine the new parts but I have access to the needed tools/equipment. I have not checked the lower ends of the shift levers but what is sloppy is the "slots" in the shifter ball or the guide pins are worn/broken. The transmission gear selector, (5 speed handle) has a lot of rotation available instead of a nice front to back and side to side motion. The transmission shifts fine, and once used to the power curve of this engine, it is not that bad. I could live with it but the cab is a bit cramped and my wife is going to attend the truck shows with me so I need all the room in the cab, (for baggage, not her) I can get!! Thanks again, Rob
  7. Hi Fred, great to see you post on the board again! The V8 really does run well now. Spent about an hour and a half yacking with the fuel injection guys about matching pump and turbo outputs today and giving thanks for their guidance with my governor. With their recomendation, I'm going to cut the fuel back just a bit as I don't want anything on a trailer painted black from the smoke!! Also wanting to install the 13 speed later this month and get some license plates, so the future is looking brighter! I'm planning to make the show at Elnora this year, (with this Mack) but first I've got to do something about the wiring. I don't feel it would be wise to trust the current installed harness. Don't expect any changes in the trucks outside physical appearance by then, I've not had much free time lately. Talk to you soon! Rob
  8. I've got an oil leak in my V8 Mack engine that is coming from one of the "buttress" bolts through the side of the block to the number three main bearing cap. My question is can I remove the bolt, after cleaning apply sealer to the threads and or a gasket and retorque the bolt? Should I remove the oil pan, and remove the main cap bolts first? Never worked on this engine other than the governor and it doesn't leak oil anyplace else. Thanks, Rob
  9. I dunno there Paul; I've sure turned down a few offers on both the Detroit, and the Mack engines. If this Detroit engine that I have was not so damn "familiar" to me, I would just leave the V8 in place. This truck really runs out well, but the front end is very sloppy due to tie rod ends being shot. Under 40MPH and it is alright on smooth pavement but above that is anybody's guess. I absolutely despise the six speed transmission because of the shifter "slop". I purchased a reman RTO-12513 from a Mack RW-613 and will try to get it installed before the end of August. Time is short right now with all the construction projects going on at work so I don't get to "piddle" in the shop much. Hope you're doing alright and making progress with your Mack. Keep me posted on the drive axle from Tulsa. Tell your uncle I said hi. Rob
  10. Well tonight I reinstalled the rebuilt governor assembly back on the truck. As king Richard used to say, "Man, What A Difference"!! There is a bit of a lengthy story to get to this point so bear with me through the details: Upon dissassembly, the flyweights were found to already have oversized pins installed and the correct bushings were no longer available, and these were worn out. In fact when the pump was rebuilt once before with new pins installed, one of the oiler holes was not lined up properly so the pin and arm was starved for lubrication from the get go. Long story short is that I rebored, and reamed the holes in the flyweight(s), made new bushings to fit the new pins, installed new springs and thrust bearing, then hand cut the top, and rear cover gaskets, (they are no longer available). The gasket that sandwiches between the governor housing and the main pump body is still available, but at a different thickness necessitating fuel rack adjustment(s). As FJH said, it was a real somebitch to get the yoke back into the fuel racks. It sure was easier to get it apart!! The engine now idles/runs steady at 725rpm with both the compressor running, and off. Off idle response is great. I need to shorten the adjuster on the throttle linkage as the engine will run much slower with this linkage disconnected. I've already run the idle adjust screw out as far as possible. It's determined the gasket at the governor housing is causing this as it is nearly 3 times as thick as the original. There is plenty of room for adjustment through the linkage. Really appreciate the help and all the pointers here. I've got about 8.5 manhours into this thing but I usually work cheap on my own stuff. Besides, I've learned quite a bit and that is basically a miracle, (the learned part). Thanks again, Rob
  11. HI Trent, hope you had a good time. Had it been next weekend I would have showed up. Your last picture looks as if you are missing a chunk of frame just back from the driver's rear tire. If that is so; I've never seen something like that before. Rob
  12. Hi Dave, I've maintained this engine for the last 17 years of it's service life and when it was time for replacement, I kept it. There are N80, green tag injectors installed. Both turbochargers are Garret T18A40's with .96 A/R on both turbine and compressor sides. They spin up really fast. The spec sheet that the vendor supplied many years ago lists the engine at 586HP at 1800 rpm. There is no listing for torque nor any curves supplied with the package. Slobbering, or "wet stacking" was never really a problem with this engine as it had "load shed" with it into a load bank. I keep it in tune to load the genset to 60% of rated capacity when running and supplying emergency power. I could go to 85% capacity but that just wears the engine much faster. I do have photos of the engine but not on this old computer. I will post a couple pictures in a bit. I can't really remember the engine number but it is a 12V-71N series and the first four of the model number are 7103-XXXX. It is a left turning engine, (looking at the rear of engine) and has a "00" flywheel housing mounted. I have purchased a very good running 8V-71 engine to switch out flywheel housings, and flywheels, etc to make the V-12 a truck engine. It will be installed into a 1977 R-795 Mack. (More on this truck in the feedback section if I don't get a couple of parts that were paid for). I've found a couple of pictures from another place I visit so I'll try to get them over here. Hey what do you know, that worked!! Anyway, I plan to use the truck for pleasure only and it will not be a real working unit. This engine has just over 6300 hours on it and has had the oil changed at 200 hour intervals since new. I suspect that unless something is grossly out of kilter, it should work well for my application. Any and all help and insight appreciated. Thanks, Rob
  13. Hi Dave, thanks for your thoughts. I had wondered about the lack of a charge air cooler on two cycle Detroits myself. I've seen in marine applications the intercoolers sandwiched between the bottom of the blower, and intake manifold and have heard they are restrictive. With the added height, they would not fit under the hood of a truck without modification. My engine is from a genset and has two T18 Garret turbochargers that are plumbed to the air boxes. It would be entirely possible to not use a charge air cooler as the engine is much higher in horsepower than I will ever need as it sets. Thanks, Rob
  14. Very "classy" working truck there Rick. A couple of fresh tires on the tag and all will be perfect. That is the kind of truck that makes real money. Rob
  15. If you are smelling the sulfuric acid from overcharging, your regulator for the alternator is bad or needs adjusted. This was a common occurence and regular maintenance interval in a earlier time. Ignition coils have either a primary resistance wire that is disconnected during the engine crank cycle, and enabled during the run cycle, or an external ballast resistor that follows the same theory. The purpose of a ballast resitor is to limit voltage to the breaker points to extend their service life. In normal operation, full battery voltage is applied to the ignition system during a crank cycle, and limited to an area between 9.25-9.75 volts when the engine is running. You can run full battery voltage all of the time, but the breaker points will not have a very long service life. If you do not have resistance wire in your cranking circuit, a Chrysler ballast resistor is easy to obtain at your local parts vendor, and easy to install. Rob
  16. That's good "food for thought" Herb. I've been around a lot of broken differentials; All single drive axle that would not move a vehicle once failed. I suppose a Mack inter axle power divider with it's full time driving ability would still power the truck forward on the opposite of the failed axle. It would reason that as the missing or broken teeth engaged and let go, the result would be quite noisy and a severe shock to the driveline. Rob
  17. While true of natural rubber, or to an extent, Neoprene, oil/grease will soften and attack rubber where polyurethane, (of which the conversation speaks of) is impervious to attack from petroleum products. I actually use silicone grease, (dielectric compound such as used on spark plug boots) for lubrication of urethane parts. It keeps the speaking to a minimum long term. Rob
  18. Hi Greg, if you would like, give me a call as I may have access to what you can use possibly? Thanks, Rob Swallows 309-219-2070
  19. I've seen several of the polyurethane bushings break the lower caps upon tightening up the bolts and nuts. This is usually the result when an impact wrench is set on high torque, and the fasteners are not drawn down evenly. I usually tighten in a four step torque process using an "X" pattern. Ultimately, these fasteners need about 1250-1400 ft. lbs. applied. It is easy to get "over zealous" to get the job done quickly. Also, be sure to lube up the exterior, and interior of the bushings before installation. This will allow them to move a bit as they compress. Good Luck. Rob
  20. I've facilitated this same repair both ways. A 3/32" 6013 rod melts at a low enough temperature as to not make the spindle a safety hazzard. Removing the spindle and chucking it up needs to take place no matter which method you choose. Two that I have welded up and machined to the proper diameter had frozen the bearings and destroyed the spindle so there was nothing to lose. To the best of my knowlege, both trucks are still in service. Rob
  21. If your tachometer is cable operated, the drive cable is binding and letting go inside the jacket. Take the cable loose from the back of the tachometer, and use speedometer lubricant to take care of that problem. If the tachometer is electronic driven, and driven by the alternator windings, chances are that a diode is blown in the alternator. Have you noticed a degredation in battery charging performance at all? Rob
  22. I'd be willing to bet the items you are asking about are all available new from your local Mack dealer. The worst enemy to plastic is the sun and heat. If you locate used parts, they will probably break, or fatique in a much shorter timeframe than new items. I'll bet you would be surprised that some parts are very affordable. Just my thoughts. Rob
  23. Thanks Mike, I contacted these folks: http://detroitradiatorcorp.com/ as far as building a radiator for me. I want to go with a "side by side" configuration, (radiator, charge air cooler) as to leave room for an a/c condensor up front yet retain the original shutters. They will build anything by request but I'm wanting a rather "custom" installation. They need the heat generation potential of the engine to build an adequately sized core. Knowing that some type of Mack chassis was factory equipt with the V-12 Detroit, saves a lot of guesswork as they have the parameters, but needed a model number to associate to. I'll keep you posted on progress. Rob
  24. Paul, I've got a technical school coming up in August at OKC. I could bring that axle assy from Tulsa to either my place, or Morgans, towards the end of August if you have no luck by then. Hauling would be "dirt cheap". Rob
  25. Hi there, what was the model number for the chassis when factory equipt with a V-12 Detroit engine on an R model? I need to get a radiator manufactured for mine and have to have some sort of baseline for fitment. Thanks, Rob
×
×
  • Create New...