-
Posts
5,644 -
Joined
-
Last visited
-
Days Won
70
Content Type
Profiles
Forums
Gallery
Events
Blogs
BMT Wiki
Collections
Store
Posts posted by mrsmackpaul
-
-
As said above
-
Congrats on the new arrival, hope all is going as planned
Paul
-
On 8/25/2020 at 10:57 AM, kscarbel2 said:
.
.
I finally got around to watching these videos
Very interesting stuff and thanks for sharing
Paul
- 1
-
Yep I'll roll with this, we need a laugh these days
And yes it would be fantastic to bring it back to life
Paul
- 1
-
14 hours ago, kscarbel2 said:
A very smooth and stylish truck
Paul
-
Kenworth had adds back in the 70's for their mid size trucks that went something like
"Most mid size trucks are lightweights built up, at Kenworth we heavy heavyweights built down"
Those Dodge Big Horns look like a lightweight built up job to me
Paul
-
PICTURES IN HISTORY 🌍
The crew of the 'USS Stickleback' didn’t expect things to end this way—rising from the depths on 28 May,1958, only to be broadsided by the hull of a friendly American destroyer, the 'USS Silverstein'. The Stickleback sank to the bottom, an 11,000-foot journey to nowhere.Now, 62 years since the sub disappeared from any radar screen—and became one of only four U.S. Navy submarines lost since the end of World War II—it’s been found again.
The sub—named for a spiny, scaleless fish native to many northern waters—was found off the coast of Oahu, Hawai’i, by the Lost 52 Project, an independent initiative to find the 52 American submarine wrecks from the World War II era. The great depth of the wreck (over two miles beneath the surface), and the fact that its precise resting place was unknown, allowed the submarine to elude discovery until now. The project found the sub by cross-referencing old records with modern sonar technology and remote submersibles, which eventually located the ship split in two at the bottom of the sea.
The Stickleback’s sinking could have been far worse. It occurred in 1958, after the sub had come out of decommission—ship retirement—to serve in the Korean War. A training exercise gone awry had caused it to plummet through the depths; when the sub managed to resurface, it found itself in the path of the Silverstein. A collision was unavoidable, yet no one was hurt, and the Stickleback’s crew scrambled onto the friendly destroyer before the sub foundered and slipped below the waves, this time for good.
Check out the link here for more info 👉 http://www.lost52project.org/Stickleback.html- 1
-
What breed of traileris that Brian ?
Paul
-
1 hour ago, Mack Ccrs 470 said:
I have a Mack 2003 ccrs 470 quantum goes good bobtail but when I load up and not go very good boost about 29 sometimes you feel loose power and won’t boost past 12 and no whistle no power like limp mode any ideas where to look
Does blow black smoke when this happens???
If it isnt blowing black smoke it would be telling me it is lacking fuel
Paul
-
So we had no idea we were independent being before mirrors were invented??
Must of been a heck of shock to who ever invented the mirror to learn he or she was some one
Paul
- 1
-
3 hours ago, kscarbel2 said:
Paul, you might be interested to watch the WW2 videos by Mark Felton. They really are quite good.
https://www.youtube.com/channel/UCfCKvREB11-fxyotS1ONgww/videos
https://www.youtube.com/watch?v=5XX9ptCNpik
Well I have learnt something new today, I never new Japan landed on Australia during WW2
Paul
- 2
-
- Popular Post
- Popular Post
#Onthisday in 1942 the battle of Milne Bay began in New Guinea.
On the night of 25 August 1942, Japanese troops landed by sea at Milne Bay. Two Australian brigades (about 4,500 men), some American engineers, and two RAAF squadrons were awaiting them. A savage battle raged along the shore, but after several days and extreme exhaustion, Japanese troops began evacuating by sea on 4 September. Of the 2,800 Japanese landed, only 1,318 re-embarked.
Allied deaths included 167 Australians and 14 Americans.
Milne Bay is remembered as the first defeat of the Japanese on land during the Pacific War. Learn more: http://ow.ly/ap1Y50B358E
Image: RAAF airmen of No. 75 Squadron sitting on top of a dugout awaiting an action against the Japanese. August 1942.
RAAF Official photograph. P02018.129Identified, left to right: 404103 Flight Officer (FO) Richard (Dick) Tweedy Holt; 404355 FO Roy Gordon Riddel (Hotshot); 403049 FO Keith Munro Gamble; FO Max Johnston (Hawkeye); 404087 FO Raife James Cowan; 402963 Pilot Officer (PO) Stuart (Stu or Stewy) Munro; 033077 FO George (Hugh) Hubert Newborne Shiells (Digger). On 27 August 1942, PO Munro, aged 21, was killed in flying battle over New Guinea.
- 5
-
That's one heck of a result there
Paul
-
Fantastic stuff, it's always good to get feed back to know if the results on these mods are going good
Sounds like another winner
Paul
- 1
- 1
-
On 8/21/2020 at 7:06 PM, harrybarbon said:
David, I enjoyed walking thru the 225 Antonov some 16-18 years ago when it was at the Avalon, Victoria Australia air show, including climbing the stairs to the flight deck, it was massive, it was lowered to minimum ground clearance and the front and rear were open, there was a very long que of people to see the Antonov, we entered from the back and out the front - 1,000's attend these shows to see, walk into and thru some magnificent aircraft and watch some real flying, including 1 jet plane similar top wing design do the 360 rollover.
I have some recollection that the Antonov did a take off, went around for a low fly thru along the main Avalon runway and then went around the bay and came in for a landing.
Also many years ago, the Antonov flew into Melbourne Tullamarine airport, my mate was a refueling supervisor, he did the refueling of the Antonov. He had the joy of a guided tour of the entire Antonov by the engineer.
I have read an article and saw a youtube video of an incomplete Antonov in the hanger in Ukraine. Is this true and correct? Article noted that if the funding could be secured to complete the Antonov, then it would go ahead.
The Antonov fly escaltors into to Sydney when Melbourne was building its first Crown casino
It couldn't land in Melbourne then for some reason and the escalators were trucked to Melbourne
The company Kone Elevators won the contract because they were the only people that could get the escaltors in the time frame required
Write ups in the paper and Im pretty sure even made it to the news on TV
Paul
-
Looks sharp
Paul
-
Is air still getting to the bags at all or is there a crook valve, if air is getting there and a bag is blown or a hose is damaged, fix that
As Mark T says "fix them and you'll see a instant improvement i ride"
Paul
- 1
-
Have a CRACKER OF A DAY Alex
-
11 hours ago, R.E.D said:
Also just got done putting the s400 on the granite along with better flowing manifold.Piping and muffler were changed to 5".Haven't drove it yet since I need to tidy up ,but I can already feel the truck's rpm climb easier..
By the way just would like to mention something if it hasn't been already said.Make sure the manifold is centered between the two cylinder heads ,other wise fuel lines won't fit..DONT ASK ME HOW I KNOW.😁🇺🇲
Great to hear a report back as to how it all worked out when you get a chance
Paul
-
Sounds like the cab has air ride and the air bag for the cab isnt inflating
Maybe a linkage has dropped off valve or the valve is fault
Hop under the truck and look at the cab for a deflated air bag or bits missing or hanging
Well walked the dog "Miss Molly" that is, my border collie
While I was walking I thought I would quickly google air ride for CH Mack cabs
And it appears that as I suspected CH Macks have a air ride cab
Now the Granite you have I believe is based on a CH cab
It should have air ride similar to this photo
And it should ride pretty good when working
The way describe that your truck is looking like its broken in half when parked would lead me to think the cab air ride isnt working at all
So I would check the air bag shown in the middle of the picture to see that its inflated
Paul
- 1
-
Is the cab suspension working correctly, I assume it has suspension on the cab
Paul
-
Vent on transmission is blocked
Oil out the selector valve would be more of air tank full of crap and oil than a gear box issue as the two arent connected
Paul
-
-
- Popular Post
- Popular Post
My daily user float (low loader) is Steco which I believe may have been a US brand
Australian made and heavy as all get out
Had it for many years and will have to fix it all up one day
These were ex army and I believe a lot went to Vietnam with our troops to shift their APC's about
I have seen photos of two APC's on the one trailer
One in the guts and the other over the back end
Paul
- 3
Dodge Road Tractors
in Other Truck Makes
Posted
When did Fargo stop existing, at a guess I would of said mid 50's in Australia
Paul