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oldspwr

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Posts posted by oldspwr

  1. After everything was cleaned up, I realized the ratio was actually stamped on the carrier.  Before I thought the only way to identify the ration was by looking at the head if the pinion when the number of ring and pinion teeth were stamped.  Here is a quick sketch of where the numbers are on the carrier...   When I called around everyone asked for the casting number, 28656, which refers to a ribbed carrier.

    M6Ffft.jpg

    The following day was supposed to be warm so I dug out all of the paint supplies and figured I would shoot the rear outside.  But I wanted to clean the inside one more time before paint.  Also, when I originally pulled the carrier, the back lash felt good and the ring gear looked good.  So I lifted it up in the air one more time to check the back lash with a dial indicator.  As I was rotating the ring gear I was looking up towards the pinion (which is sort of buried in the carrier) and caught a glimpse of something that looked BAD.  At that point I decided to pull the pinion cage to get a closer look...

    zMBuFJ.jpg

    Damn...  I still can’t believe that I didn’t feel this in the back lash but these things happen.  I also didn’t see any chuck in the bottom of the housing (and I wasn’t really looking either...) since it was raining pretty good and we were trying to get out of the weather.  Should I have looked at it better before I cleaned it?   Sure, but hey these things happen...

    So at that point I started looking for another set of gears.  But at least this time I had more information, like the Eaton number on the ring gear, 41962.  After a quick Google search of this number, I found a set of gears in Toledo OH (same place that had the carrier years back).  They listed the ring gear as 41962 and the pinion as 48820.  This is when I posted a wanted ad on the message board hear and well as on a few groups on FB.

    More to follow...
     

  2. Then using some 2x6’s and some extra heavy duty casters I had, I made a quick ‘box’ to be able to move the pumpkin around.  Besides, I would need something to move or store the 6.71’s when I removed them...

    1TKp8C.jpg

    c2NFmY.jpg

    Then with some ‘help’ from Maddie I was able to roll the pumpkin outside...

    51QPNN.jpg

    And get everything cleaned up...

    k1J7F1.jpg

    More to follow...
     

  3. One of the first things I need to do was change the gears in the truck  Almost since I bought the truck, my Dad and I had always talked about finding a taller set of gears to see if it would help the truck move along a little better.  Right now the truck has 6.71/9.13’s and based on several 155W specs sheets I have collected,  5.43/7.39’s and 6.14/8.36’s were also available.  So I put a quick spreadsheet together a numbers of years ago to compare the ratios and  5.43’s would lower my RPM’s from about 2150 to 1800 at 55 mph.  

    D5jwF4.jpg

    When I started looking for gears a while back, I hit a number of roadblocks since I didn’t have enough information.  To make matters worse, the specs list the rears as both 20501 and 20503 and I was not able to find these numbers anywhere in any of Eaton’s older literature.  A few guys asked for the casting number (28656) and I was able to find a set in Toledo OH but they wanted $1500...  ouch...  Then about 3 years ago I found a rear out of a 257 that came with a 180 Cummins.  The casting number matched my rear (28656) so I bought the rear and set if off to the side.  On a side note, I do have a spec sheet for the H257T and it only list the only available rear ratio as 5.43/7.39 but they call the rear an R454.

    rUZFf5.jpg

    When I decided on the Cummins upgrade a few months ago, I figured I would change the gears first just to see how they worked with the Continental.  If I remember correctly, I talked to the owner of the Green Apple Express 257 a few years ago and he said he replaced his gears with 5.43’s and it made a world of difference driving the truck with the 572 Continental.  So I decided to pull the pumpkin from the rear and get it ready to install in the truck.  But that was easier said than done...  I had the rear sitting on a drop deck trailer on the far side of yard and at the time I wasn’t able to bring the trailer over to the garage to lift the pumpkin out with the fork lift.

    lOx8jq.jpg

    So we wound up using the cherry picker and my 4 wheeler along with a utility cart, in the rain I might add, to get the pumpkin in the garage...

    4J98ch.jpg

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    More to follow...
     

  4. Thanks for everyones comments, I appreciate them!!!

    When we last left off I resolved the oil pressure issue I had.  One of the things I noticed with this truck was that it was very difficult to drive smoothly.  In other words when leaving from a dead stop, it seemed as if you either gave it too much throttle or not enough, and when you had it moving it was surging.  I met Dave Crump at Macungie and he explained that my problem was common to the earlier Cummins PT pumps. 

    This was the pump that was originally on the engine...

    vqZwlm.jpg

    After a few more discussions I sent him my PT pump and he wound up sending me back a later AFC style pump.  He set it up for an NH280 which was the highest horsepower non piston cooled Cummins (I believe...)  And this is the later style pump he sent me...

    djZj9H.jpg

    To install the newer pump I had to pipe in an additional fuel return line and use a short extension to feed the fuel line that runs to the rear of the block.  I also had to relocate the air intake that went from the air intake manifold to the air compressor since it now interfered with the tach drive cable.  While waiting to get the pump back I also replaced all the fuel lines with new push to lock lines...

    SPiNVX.jpg

    And I also drained the fuel tanks and cleaned the fittings and valves...

    yOvCKf.jpg

    Once all of the lines were on as well as the new pump, I filled and reinstalled a new fuel filter and topped off the injection pump.  I really struggled with getting the truck to run and had no throttle response as well.  Turns out I still had a ton of air in the system.  To help bleed all the air out, I took an old fuel cap that had a busted lead plug in it, drilled and tapped if to 1/4" NPT and installed an air compressor fitting. 

    PfURqy.jpg

    I then removed the pipe plug from the top of the PT pump and used a valve I put together to air the trucks up...

    GdEebQ.jpg

    More to follow...
     

  5. When I last left off I had just finished working on the air inlet piping from the air filter to the turbo.   I had decided not to install the drag link or pitman arm until the truck was just about ready to be driven because without these items it allowed me to get closer to the motor.  But since I was 99% done with everything I decided to install them.

    rSR9cJ.jpg

    After I installed them I realized the drag link between the steering arm and the pitman are was not even close to being parallel with the frame.  The pitman arm still had to get pressed on at least another 1/4" but even with that I wasn’t close.  I crawled under my Dad’s 361 and that drag link was fairly parallel to the frame but it also had a ‘job’ in it.  At that point I remembered that Russ had given me a 1/2" spacer with a Sheppard box. 

    QKr62i.jpg

    I did have some room between the steering box and the radiator so I decided to install it.  Instead of removing everything, I cut the spacer in half and then installed one half at a time.  In the meantime I stopped to check out the progress on Paul Polcha’s 761 and his setup looked very similar to mine so I was comfortable with installed the pitman arm on the rest of the way...

    2M3OVJ.jpg

    After I was done moving the steering box, connecting the drag link to the steering arm and adjusting the ball and socket spring end, I slid the steering shaft on.  Once I did I realized that all the U joints were very tired and the bearing at the bottom of the fire wall was tight.  For some reason I completely forgot about these.  Fortunately Napa has the U joints in stock (part number UP861 or Neapco 1-1475)...

    After I disassembled the shaft I realized the u joint cups were spinning in one of the joint ends (the yellow one) but I was able a better one in my collection...

    sKitIU.jpg

    The other bearing I mentioned is located at the bottom of the firewall where the steering shaft goes through.  These are the parts that hold it in place...

    OCcDI7.jpg

    This bearing is held in place with a lock collar and set screw, just like the shafts on my snowmobiles.  This bearing is a Fafnir RA100RRB and it comes with the lock collar...

    SVtOwQ.jpg

    I wound up sandblasting all the parts, giving them a coat of black paint and reassembled everything.  

    More to follow...
     

    • Like 1
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  6. Hi Paul... I have CB's in all my Brockways but really don't hear much on them these days...

    Ok it’s time for another update!

    Another thing on my list of ‘things to do’ was fix the Fuel Level gauge.  I had filled the tanks up and realized the gauge still read empty.  Brockway used Stewart Warner gauges which in turn meant they also used Stewart Warner fuel sending units.  These units are rated at 240 ohms empty, 33 ohms full.  To start, I disconnected the wire on the sending unit and then checked the resistance with a multimeter.  I had infinite resistance so I determined the sending unit was bad.  I also checked the continuity between wire on the sending unit and the back of the gauge just to make sure it wasn’t a wiring issue either.  I wound up buying a new Stewart Warner sending unit from Summit Racing for $30, part number SWW-100438...

    Here are some pics of the new one with the old one...

    NzCriu.jpg

    And then I found this!  It looks like besides the rheostat part going bad, the float spent a lot of time sitting on the bottom of the tank!!!

    FsWan6.jpg

    The screws were a little challenging to get out so I cleaned the holes with a 10-32 tap (with some grease to prevent the stuff from falling in the fuel) and then installed the new sending unit with some new screws...

    GzoSMC.jpg

    Another thing I decided to work on was the air intake tubing from the Farr to the turbo.  There was some overspray on the 5.5” metal section and the rubber pieces as well...  

    qK0QRq.jpg

    The first thing I did remove everything and add some rubber edge molding to the hole.  I usually buy this molding from McMaster Carr...

    xmeGa6.jpg

    More to follow...
     

    • Like 2
  7. Here is a list I put together a while back that lists the model numbers of the various types of Brockway cabs.  Not many folks are familiar with this so I figured it would help.  Steve Skurnowicz provided a lot of help on this list as well...

     
    Model 31 Trafficab with Folding Doors
    Model 35 Metropolitan Cab
    Model 41F and alphabetically lower one piece push out windshield
    Model 41G and alphabetically higher one piece gasketed windshield
    Model 50 is the wooden framed Deluxe cab with the three piece windshield and narrow cowl
    Model 51 is the model 50 with a sleeper
    Model 52 is the Deluxe three man cab
    Model 57A - 550
    Model 60 is the Deluxe all steel cab with the three piece windshield
    Model 61A-61J are all steel sleeper cabs
    Model 65B - 358 & 359
    Model 67 - 358 & 359 3 man cab
    Model 68 - 360 and 361
    Model 75 - 758 & 759 (depending on engine) (Sheller Globe Cab)
    Model 76 - 758 & 759 (depending on engine) (Sheller Globe Cab)
    Model 78 - 760 & 761 
    Models 50/86 - 457 & 459
    Models 763 / 773 / 783 / 793 - 776 (depending on engine) (Sheller Globe Cab)
     
    I can add pics if that would help...
     
    • Like 2
  8. Well I have been able to finish up a few loose ends.  A while back I mentioned I wanted to reconnect the existing Kysor alarm system.  I was able to find the correct sending units on eBay.  I was unable to find a one wire pressure switch for the oil alarm but I did find a 2 wire.  All this means is that I had to run 1 of the wires to ground.  On the water side, I found the correct Kysor alarm temperature switch but needed to buy a 3/8 to ½ face bushing so that the sending unit went into the water jacket far enough...

    NRFzCm.jpg

    7hdIpn.jpg

    For the temp sending unit, I ran the wire in the same loom as the temp gauge sending unit.  For the oil pressure unit, I ran the wire along the driver side frame rail and into the cab.  Once the wires were in the cab I made the final connection to the bell.  Once everything was done, I turn the key on and the light came on but the bell sounded sick.  I guess from not ringing in a number of years!  But after a minute or 2 it sounded much better.

    The next thing I worked on was some of the dash wiring.  Surprisingly it was in decent shape but I did find a few issues.  One of the circuit breakers was bad so they moved the load over to another breaker.  I was able to fix that and replace the breaker.  I also decided to add 4 fuses, one to replace the Jake fuse that I fed from Ignition Power, one for the PTO light that I fed from accessory power, one for a CB that I fed from accessory power, one for a future cigarette lighter that I fed from constant power.  I will mount the extra cigarette letter in the glove box so that I can charge a phone, etc. when I’m at a show.  Then my phone will be out of site...

    This is not a great pic, but I bundled the fuses together and they fit right behind the plate with the Kysor decal...

    Qvq5Z8.jpg

    I had always wanted to put a CB in the truck but waited until now.  I had a 1976 23 channel Midland that my Dad had used years ago and thought it would be ‘fitting’ for this truck.  But I also thought that in the future I may want to install a newer 40 channel Cobra.  Since the Midland is narrower than the Cobra and I didn’t have the original Midland mounting bracket, I made my own.  I based this off of the new Cobra one I had...

    Uid22Y.jpg

    Then I made a plate from some 1/8” plate that I had.  I made this so the face of the CB would be flush with the dash.  But I also made it wide enough to mount a Cobra in the future...

    gHxOJQ.jpg

    The one thing I didn’t have was a Midland mic, so I could the correct one on eBay for only a few bucks.  The truck already has a CB mic clip mounted to the dash so I left that in place and reused it.  And this is what I wound up with...

    zDy5dT.jpg

    For the antenna, I decided to mount it off of the driver side mirror.  On all the Brockways I have used a Kenworth antenna mount from Walcott CB, part number KWM.  This is a stainless piece as well.  It comes with an antenna base but in my experience they continually come loose.  I usually replace these with Francis 300-CBM102 Stainless Steel CB Radio Antenna mounts.  These are also stainless.  The only problem is that they are no longer made in America...  

    fjHY78.jpg

    IqZnbt.jpg

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    I also used a 24” black Firestik II FS2-B 5/8 Wave 300 Watts tunable tip CB Antenna.  These are nice since you can adjust your SWR’s with the adjustable tip.  Not terribly period correct but short and unobtrusive. Keep in mind that my Dad always carried a ‘CB box’ with him at Roadway so I spent a lot of time over the years making boxes, fixing CB mics, repairing antenna cables, etc.  In fact one time he was driving under a bridge and lighting hit the bridge and transferred over to the CB antenna and into the CB.  It actually shut the truck right off but he was able to restart it.  It destroyed the antenna and cable but all it did was blow out the diode on the power side of the CB.  These are the diodes they use in case someone reverses the polarity on the CB when they connect them.  I still have the fried antenna cable in the garage :)

    That’s it for now!
     

  9. In another post I had asked about the correct location for the Jacobs engine brake switches.  Some folks have them mounted on the passenger side of the dash but the most common place seems to be on the left side of the speedo and tach.  I also have a 1974 300 series dash and it has a blank plug in this place along with a blank fiber optic tag.  So I decided this was the best location.  I also was able to find the correct older switch plates.  These came from Courtland Truck Works who specialize in Peterbilt restorations.  I taped them in place first...

    pZAcbC.jpg

    The switches were originally mounted very tight to the tractor protection valve and this is how they were wired so I corrected this as well...

    ruIk2b.jpg

    And this is the finished product...

    qIQaJX.jpg

    I’m happy with this location and it matches were I put the single switch in my Dad’s 361.

    I also dug out the original protection valve dash plate from my Dad’s 361.  This still was in decent shape and had the factory decal on it as well...

    k4vrqf.jpg

    And I wound up replacing the original plate that had the extra holes drilled in it for the switches...

    AkhLQE.jpg

    Well that’s it for now...
     

    • Like 2
  10. So my last roadblock was to try to figure out what to do with the seam in the middle.  I was able to salvage a few small scraps of fabric from these pieces...

    zfrZcT.jpg

    Using one of the scrap pieces, I glued it to a pieces of 1/8” aluminum and then clamped it overnight...

    KS2gRE.jpgL]

    It looks dirty but it did clean up well.  The next day I screwed it in place with some #4 SS screws...

    ZUtYEm.jpg

    And this is what I wound up with...

    Ee2LlP.jpg

    The last piece of the headliner I needed to fix was the center bar that holds the headliner in place.  Russ told me that when he got the truck there was an antenna mounted in the middle of the roof and they drilled a hole right through the center of this piece... 

    n2SUe6.jpg

    Well almost the center of the piece...

    RvtqkB.jpg

    I cleaned up the hole with the angle grinder and the cut a piece to fill the hole in...

    EfQSsn.jpg

    Then I was able to weld the plug in and grind it smooth...

    63f5VV.jpg

    And then I sandblasted it...

    KjZ2mp.jpg

    I gave it a few coats of DupliColor’s Detroit Diesel alpine green and should be able to install it this weekend!

    That’s it for now!
     

    • Like 1
    • Like 1
  11. Once the headliner was down I found a few wiring issues (and a handful of plastic hitch hikers!!!)...

    mVI9L4.jpg

    qFo3U4.jpg

    One thing to mention with the cab lights is that the 3 middle lights are controlled separately from the 2 outer.  I used a factory early 358 wiring schematic to help me figure out a few wires.

    I like to crimp, solder and heat shrink all my connections so I decided to fix the wiring while I was at it.  I also added grommets to each of the holes the wires passed through for the cab lights.  Once I was done with the wiring I reinstalled the headliner with the new screws.  There were also 2 pieces that were made to fit in above the front ‘package’ tray.  I’m not really sure how these were made to fit so I decided to make them work regardless.  My first though was to install them on the outside of the lip just like the side pieces.  I also did this on the 155W and my Dad’s 361.  

    6qbqDS.jpg

    But there wasn’t enough material to wrap around the bottom of the fiberboard it was glued to.  It’s my understanding that these were originally installed behind the lip.   

    MNILSZ.jpg

    I decided my best option would be to glue these to a piece of luan...

    aT0QjN.jpg

    These pieces are tapered, meaning the middles are taller than the ends.  So I had to cut these ends off...

    pohmydJRj

    Once the luan wood was trimmed to fit I used some Gorilla glue to attach the fiberboard to the luan and then clamped it between 2 pieces of wood...

    uWjMUH.jpg

    Tk6gYF.jpg

    And this was the end result...

    zpPVa7.jpg

    More to follow...
     

    • Like 1
  12. Paul, both the 270 in the 68 Brockway and the 335 in my 76 Brockway have compression releases...

    I wound up using a large black knob I had and it pulls fine.  Our 761 has the same knob in the dash and that’s what I based this on.  I wound up using a stock plate from a dash I bought from the junkyard a few years back.  The dash wound up in my Dad’s 361 since it was pretty much original without a ton of extra holes drilled in it...

    R9Hd0Q.jpg

    In the pic above you can see the plate with the large lamp for the Kysor system.  Long after the decal fell off a hole was drilled into this plate to mount a switch to control a fan.  I wanted to bring it back to original so I removed the plate and welded the hole in, being careful not to generator too much heat to burn the original dark green paint...

    3KVwuc.jpg

    Once I was done filling the hole I painted the area front and back and dug out one of the reproduction Kysor decals I had made a while back...

    P6Ga6g.jpg

    And here is the finished product back in the truck...

    0p9z7p.jpg

    As you can see this is drifting from my power steering install but that’s ok...

    The next thing I decided to work on was the headliner.  Russ had a guy in Saylorsburg make a new headliner based on the original pieces he gave him.  He had a hard time getting it to fit well so I figured I would tackle that next.  For hardware, someone had installed 6/32” rivnuts in the mounting holes.  These really don’t work well for this application since the screw needs to float a bit in the hole.  Some of them were cross threaded also (probably because of the installation tool) so I drilled them out.  I replaced them with this Balkamp #8 U spring U nuts, part #665-1955.  

    hhwL9D.jpg

    For the screws, I was also able to pick up the correct screws from Napa, but I have to dig up the Balkamp part number.  But they are the same as these Dorman 961-235 screws...

    egg79P.jpg

    More to follow...
     

    • Like 1
  13. While I was working on the compression release I decided to replace something else.  The fan support bracket that is mounted directly underneath the compression release bracket had (3) separate spaces under each bolt to compensate to the jake height. I decided to remove these spacers and make (2) new ones...

    This is what I started with...

    pnzx7dqsj

    And these are what I made...

    pnb3SXRcj

    And here they are installed...

    pmB52yGnj

    Well that’s it for now...

    • Like 1
    • Like 1
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